Hiya
I've cleaned up my wastegate/ actuator rod joint this morning. The joint moves nice and smooth now and I've set the calibration boost to 0.3 bar (it needed adjusting several turns in).
The car runs much smoother now but is overboosting so something isn't right :-(
I'm wondering if I now need to reset the system to allow the CPU and TCV to re-learn the new setup, or if in-fact by winding in to the supposed correct calibration setting, it is now no longer capable of venting sufficient boost?
The wastegate itself seems to move through nearly 180 degrees (with the actuator arm removed) but has no spring resistance.
Grateful of any advice before I wind the rod back out for safety.
TIA
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